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4.4 System Evaluation and Capacity Analysis for Northeast Areas <br />A 20-year capacity analysis of the TH 169 Lift Station was completed to assess if this lift station can be <br />used to pump wastewater generated in the northeast study area. If the TH 169 Lift Station is used to pump <br />wastewater generated in the northeast study areas, its peak hourly flow is projected to increase to 2,200 <br />and 2,300 gpm when the northeast study area is fully developed. This flow will exceed the lift station's <br />existing firm pumping capacity by 540 to 640 gpm. Although this flow increase would trigger upsizing the <br />TH 169 Lift Station to serve the study area, a capacity increase would not be required initially. <br />The TH 169 Lift Station was originally designed with space to install two (2) additional pumps. Therefore, <br />additional pumps could be installed to increase the lift station's pumping capacity. Installing one (1) <br />additional 1,200 gpm pump would increase the lift station's pumping capacity to 2,860 gpm, which would <br />be sufficient to pump the wastewater generated in the lift station's existing service area and the northeast <br />study area. Installing two (2) additional 1,200 gpm pumps would increase the lift station's firm pumping <br />capacity to 4,060 gpm. Installing a second 1,200 gpm pump could be done if large developments beyond <br />those planned for the study area are expected for the lift station's service area in the future. <br />The TH 169 Lift Station has a 1,745-ft long forcemain. Most of the forcemain (1,470-ft) is 14-inch in diameter <br />and the remaining 275-ft is 16 inches in diameter. Forcemains are typically designed to maintain flow <br />velocities between two (2) and five (5) feet per second (fps) to avoid particle settling. Depending on the <br />application, velocities of up to eight (8) fps could be acceptable. Although higher velocities are sometimes <br />acceptable, they also result in higher pipe friction headloss. Headloss in a forcemain is defined as the <br />reduction in energy of the water as it moves through the pipe. High headloss and velocity indicates a <br />forcemain is undersized for the flow that is conveyed. An undersized forcemain that generates high <br />headlosses will also increase the energy cost to operate the pumps. In order to keep energy costs <br />reasonable, forcemains are usually designed to maintain headlosses below 10-ft per 1,000-ft length of <br />forcemain. The wastewater velocity and headloss through the TH 169 forcemain were evaluated under <br />three different scenarios: existing pumping conditions, addition of one 1,200 pump, and addition of two <br />additional 1,200 gpm pumps. The results of this analysis are summarized in Table 4.8. <br />Table 4.8 — TH 169 Capacity Analysis for Existing 14-inch Forcemain <br />Scenario at TH 169 Total No. Firm Pumping Wastewater Headloss <br />Lift Station of Pumps Capacity (gpm) Velocity (fps) (ft/1,000 ft)�'� <br />Existing Conditions 2 1,660 3.46 3.0 <br />One Additional Pump 3 2,860 5.96 8.3 <br />Two Additional Pumps 4 4,060 8.46 15.9 <br />(1) I he roughness condition ot the existing torcemain is unknown and assumptions were made to calculate the <br />headlosses. <br />As summarized in Table 4.8, the existing 14-inch forcemain could potentially still be used if only one <br />additional 1,200 gpm pump is added. However, serious consideration should be given to installing a parallel <br />forcemain if a second 1,200 gpm pump is added in the future. A more detailed forcemain analysis should <br />be completed in the future to identify if the existing forcemain can be used before installing additional <br />pumps. Upon discussing the use of the TH 169 Lift Station with City staff, it was decided not to use this lift <br />station to convey wastewater generated in the northeast study area. <br />Regardless of whether the existing TH 169 lift station will be used to pump northeast area flows, wastewater <br />flow generated in the northeast study area will need to be treated at the City's VWVfP. Given the plant's <br />existing wastewater flow, it appears that the existing wastewater treatment plant has sufficient capacity to <br />treat wastewater generated in the northeast study area. <br />4.5 Recommended Sanitary Sewer Infrastructure for the Northeast Areas <br />The recommended sanitary sewer collection system layout and sewershed distribution to serve the <br />northeast study areas are shown in Figures A19 and A20 in AppendixA, respectively. The sanitary sewer <br />layout was preliminary designed based on the following criteria: <br />Feasibility Report <br />Northeast & Northwest Urban Service Area Expansion Study <br />City of Elk River, MN <br />WSB Project No. 020010-000 <br />Page 18 <br />