Laserfiche WebLink
City of Elk River Local Option Sales Tax (LOST) The successful referendum to create a <br />LOST has an operational and financial impact on ERMU because of our billing system. <br />The LOST will apply to some, but not all sales through ERMU. To implement this, ERMU <br />worked with NISC to create custom software updates that were successfully <br />implemented October 1, 2019. <br /> <br />Annual Business Plan and Budget Presentation Improvements Per the direction of the <br />commission during the Strategic Plan and 2018 Annual Business Plan Results review in <br />February 2019, staff had developed and implement a 20-year capital improvement plan <br />to be incorporated with the budgeting process. Additionally, staff implemented <br />formatting and presentation improvements so that the different sections of the budget <br />were presented in a similar format for improved readability and so that the annual <br />budget formatting was more similar to the formatting of the monthly reports. <br /> <br />Review of the 2019 Annual Business Plan <br /> <br />The purpose of reviewing the 2019 Annual Business Plan is to evaluate the budget as a tool in <br />addition to performance. By evaluating the usefulness of the tool, staff will be better able to <br />provide monthly information and reports to help the commission evaluate the organization <br />health and direction. Understanding and exploring the areas of risk and sensitivity factors <br />improved the governing set policy redirecting an organization toward the short <br />term and long-term goals. The Annual Business Plan review should help the commission identify <br />areas of higher risk, evaluate options to mitigate risk, establish their comfort level with risk, and <br />help the commission clearly communicate expectation in handling the risk. <br /> <br />Overall Electric Utility performance for 2019 was positive on a year where sales were down <br />because of weather and the 5% rate decrease. Unaudited financials indicate that electric <br />margins significantly outperformed budget ($1,593,658 budget, $2,870,619 actual). While <br />revenue performance was 1% lower than budgeted due to weather and the 5% rate reduction, <br />the annual expenses were 5% lower than budget. And net to reserve was higher than budgeted <br />($503,296 budget, $2,970,629 actual). This was our first full year purchasing power from <br />Minnesota Municipal Power Association (MMPA). <br /> <br />Overall Water Utility performance for 2019 was positive even when considering weather. <br />Unaudited financials indicate that water margins outperformed budget (-$144,494 budget, <br />$340,866 actual). Revenue was up 9% ($2,768,491 budget, $3,019,809 actual) while annual <br />water expenses were down by 8% ($2,912,985 budget, $2,678,943 actual). And net to reserves <br />was higher than budgeted ($522,399 budget, $1,157,062 actual). <br /> <br />An overview of 2019 budget verses actual (unaudited) for both electric and water is provided in <br />the attached summary. <br /> <br /> <br /> <br /> <br />______________________________________________________________________________ <br />Page 8 of 9 <br />91 <br />