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6.7.ERMUSR 04-17-2008
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6.7.ERMUSR 04-17-2008
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City Government
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ERMUSR
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4/17/2008
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Adding to the magnitude of PCA charges is significant growth in member energy sales beyond budget forecasts. <br />Heating loads continue to grow, notably in the dual fuel program. Rates for this program fall far short of <br />incremental costs, so the faster the growth in dual fuel sales, the more upward pressure will be placed on t' <br />general service rate and PCA. We must address this rate issue prior to the next heating season. <br />Please be assured that we are doing everything within our power to control these costs, but at the same time, be <br />aware that much of these costs are uncontrollable due to higher than budgeted member energy usage. Based on <br />what we are seeing, we must put much greater emphasis on our conservation programs. At the senior staff <br />strategy session last week, we concluded that we should regard conservation as our first fuel. We will also <br />continue to maintain plants to assure improved reliability during peak energy usage. <br />With the Coal Creek Station Unit 2 forced outage lasting through March 7, the probability for continued PCA <br />charges through the first quarter of 2008 is high. Natural gas prices, a primary driver of purchased power costs <br />in the MISO market, have been unfavorable during the outage. The graph below shows the gas price trend for <br />the past few months. <br /> <br />ib.'4 12 ~6 t0 :24 7 2i 4 id 3 it <br />OCT Oi WCC~vv OEfi .lAf~•08 f~8 MAR <br />As of 03! R ~ R}$ ~ Hu~~troow <br />X15 <br />i~ <br />105 <br />10 <br />45 <br />85 <br />4 <br />P5 <br />T <br />65 <br />Coal Creek Station <br />Unit 2 was off line for approximately two weeks (last week of February and first week of March) due to <br />hydrogen leakage in the generator. The leaks were found to be in the clips that attach to the generator bars <br />rather than in the hoses that were a problem a few years ago. GE has identified the problem as a corrosion issue <br />with the brazing material used in the attachment. Five leaks were fixed during the outage. The unit was back on <br />line and is performing well at this time. Additional investigation with GE will be done to determine long term <br />solutions. <br />The effect of the Coal Creek Station outage alone on the February PCA is about $4.SM. We expect the effect on <br />the March PCA to be about $4.9M. <br />
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