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Page 2 <br />Regular meeting of the Elk River Municipal Utilities Commission <br />October 12, 2010 <br />started in the near future by an independent parry to get the Jackson Street water tower on the National <br />Register. The grant money of $2650 has been received from the state to pay for this. No action taken. <br />4.2 Power Supply Options / Resource Planning Update <br />Connexus terminated the 10 year rolling "all requirements" power contract with ERMU in <br />September of 2008. In April 2010, The Utilities Commission authorized entering into Phase 1 of a <br />resource planning study with a coalition which includes Central Minnesota Municipal Power Agency <br />(CMMPA) as a participant. In September 2010, the Utilities Commission authorized entering onto <br />Phase 2 of a resource planning study which includes the release of a Request for Proposal. <br />On September 28, one of the participants announced they would not be participating in Phase 2 <br />of the resource planning study. A reallocation of costs was done and the cost for ERMU changes <br />from $19,444.44 to $25,000. ERMU's future cost for Phase 2b changed from $8,334 to $10,714. <br />This change has delayed the process because many of the participants need to obtain approval from <br />their governing bodies. ERMU staff has informed the Resource Planning Coalition that they will <br />participate in Phase 2 at the $25,000 contingent upon all other remaining participants also agreeing to <br />participate in Phase 2. Troy Adams said there would be a conference call on Friday and he would find <br />out more information. John Dietz voiced his concern and asked Troy Adams to contact the <br />Commissioners to let them know the status. Jerry Gumphrey commented he did not have any <br />concerns moving forward as long as no one else pulled out of the study. Peter Beck suggested Troy <br />Adams send an e-mail to the Commissioners on Friday after the conference call to give them an <br />update rather than calling each Commissioner individually. If at that time there needs to be further <br />discussion, a special meeting could be called. <br />5.1 Review 2011 Expense and CIT Budget <br />Troy Adams reviewed the 2011 expense and CIP budgets. Great River Energy (GRE) is still in <br />the process of finalizing their 2011 wholesale power rates. GRE is going through an extensive <br />process of budget cuts to be able to achieve a 4% wholesale power cost increase. Due to GRE's <br />budget cuts it is assumed that there will be no reimbursement from them for some of the conservation <br />improvement programs (CIP). Discussion followed regarding the recommended electric rate structure <br />and changes to the rebate program ERMU currently offers. The water department is recommending <br />the water usage rates stay the same but to raise the water connection charge from $2,500 to $3,000 per <br />unit and hire an employee to replace the one that left in 2009. Further discussion followed regarding <br />the Reserves. <br />5.2 Review and Consider 3'a Ouarter Write -Offs <br />Staff is recommending approval of the third quarter write-offs totaling $9,100.82. Over $2,000 <br />of this will be sent to a collection agency, and over $6,800 of it will be assessed this fall. <br />